Ed McDonnell
Member
When I first got my microlux 7x16 lathe the tailstock was out of alignment with the headstock enough that when turning a 3" long cylinder the diameter varied by 0.01" over the length of the piece. Great if I wanted to turn tapers, but I didn't, so not so great.
After playing around with the horizontal adjustment on the tailstock I got it to within 0.004" over the 3" length. Not too bad, but I could do better on my wood lathe by hand!. The vertical alignment was off and I haven't had the time to try to adjust it until this weekend.
I needed to lower the tailstock, so I disassembled the tailstock and removed a little bit of metal from the bottom of the top piece of the tailstock. Not wanting to end up having to use shims to raise the tailstock or buy a new tailstock ($80), I only took off a tiny bit at a time. Disassemble, remove metal, reassemble, test, repeat. After doing this countless times I can now disassembe or assemble the tailstock in under a minute. Not sure what I can do with this newly learned skill, but I've got it if I need it.
If I had a mill this would have been a very simple quick task. Rubbing the tailstock on sandpaper on a flat surface and guessing about how much I was taking off took a lot longer.
It took me almost 6 hours to get it completely aligned. I can now turn a 3" long cylinder with less than 0.001" change in diameter. I wanted 0, but we can't always get what we want.
I used a razor blade between centers to indicate the direction of adjustment needed. I'm surprised how close to zero I was able to get with such a low tech approach.
The other thing I learned is that the scale on the compound is not real accurate. I am going to make some angle gauge blocks for setting the angle on the compound when I need it.
The only thing left that I want to work on is the backlash in the cross slide. It's not too bad, but I would like to eliminate as much as possible.
What kind of adjustments have you made to your lathe to get the performance you wanted?
Ed
After playing around with the horizontal adjustment on the tailstock I got it to within 0.004" over the 3" length. Not too bad, but I could do better on my wood lathe by hand!. The vertical alignment was off and I haven't had the time to try to adjust it until this weekend.
I needed to lower the tailstock, so I disassembled the tailstock and removed a little bit of metal from the bottom of the top piece of the tailstock. Not wanting to end up having to use shims to raise the tailstock or buy a new tailstock ($80), I only took off a tiny bit at a time. Disassemble, remove metal, reassemble, test, repeat. After doing this countless times I can now disassembe or assemble the tailstock in under a minute. Not sure what I can do with this newly learned skill, but I've got it if I need it.
If I had a mill this would have been a very simple quick task. Rubbing the tailstock on sandpaper on a flat surface and guessing about how much I was taking off took a lot longer.
It took me almost 6 hours to get it completely aligned. I can now turn a 3" long cylinder with less than 0.001" change in diameter. I wanted 0, but we can't always get what we want.
I used a razor blade between centers to indicate the direction of adjustment needed. I'm surprised how close to zero I was able to get with such a low tech approach.
The other thing I learned is that the scale on the compound is not real accurate. I am going to make some angle gauge blocks for setting the angle on the compound when I need it.
The only thing left that I want to work on is the backlash in the cross slide. It's not too bad, but I would like to eliminate as much as possible.
What kind of adjustments have you made to your lathe to get the performance you wanted?
Ed